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102249。。。TH311A1000-3932201304-0485-051。。20802。。———3。3。。。1*14Q0Q1R0R1n0H0H1ABH1OQ1B。R0n0n1H0H2ACH2OQ1C。SH1OQ1B>SH2OQ1C5~8。1920%Q、HnQ1Q0=n1n0H1H0=n1n()025844.*2012-11-1920976193Q0Q1H0H2。。。“”。。22。2。2“1”“2”ρgz1+p1+ρu122+Δp=ρgz2+p2+ρu222+ΔpL1u———z———“1”Δp———ΔpL———。10ΔpQΔp=a+bQ+cQ2a、b、c11ΔpL=bL1-2Q2bL1-2=λl1-2+∑leD+∑()ξ·ρg21π4D()22p2=c-bL-ρ2A2Q2+bQ+a-ρgz2-z122“3”“4”p3=bL3-4-ρ2A2Q2+ρgz4-z332、3、。2Q0=0.05m3/sH0=55mn0=2950r/mind=0.3m3a、。H=H0+bL1-4Q2H0=Δz+Δpρg。p2'=bL1-4-bL1-2-ρ2A2Q2+ρgH0-ρgz2-z14ΔpcΔpc=bcQ2p3'=bL1-4-bL1-3-bc-ρ2A2Q2+ρgH0-ρgz3-z15bc=ρkvc2。4、5、。85%3b。0.36MPa0.02m3/s。、1。684403、1Q↑Q↓p↓p↑p↑p↓p↑p↑p↓p↓2“3”———gz+pρ+u22=66。G1G2G1<G2。u2。23。。1Q1Q2Cn1D。Q1n1C。Q1R1B。。。12Γt=-·Γ珖u+G-FF———G———G=p+ρgzΓ———Γ=ρu。L13ρLdudt=12ρu12-12ρu24+p1-p4+ρgz1-ρgz4-ΔpL+Δp-Δpc7ΔpL=FL。Δpc=bcQ28Δp=a+bQ+cQ29ΔpL=bLQ2107~10。7~10Q=0.045m3/sQkkvckQp47844.Qsks=2Δ珋pck0/珋kvc2bL珚Q-b+2c珚Q+2Δ珋pc/珚Q·1T1s+1Qsp4s=-12bL珚Q-b+2c珚Q+2Δ珋pc/珚Q·1T1s+1T1=ρL2Δ珋pc/珚Q-2c珚Q-2bL珚Q+bAsAs。1415Q=-Bn-Bn2-4ACn2+4AΔ槡p2CA=an02B=bn0C=c。QnQp4Qsns=BD+4AC珔n-B2珔n2C2bL珚Q-D·1T2s+1Qsp4's=-12bL珚Q-D·1T2s+1T2=ρLA2bL珚Q-DD=B珔n+2C珚Q。Qsks=0.000863.65s+1Qsp4s=-1.1×10-73.65s+1Qsns=0.001928.60s+1Qsp4's=-6.71×10-78.60s+110s26s。Matlab/SimHydraulic216。0.045m3/s0.050m3/s35s0.10MPa0.15MPa。4。。。。44Matlab/SimHydraulic。。1.M.2.2004240~242.2.J.2010817~19.3.J.20091618~11.4BortoniEDCAlmeidaRADVianaANC.Optimi-zationofParallelVariable-speed-drivenCentrifugalPumpsOperationJ.EnergyEfficiency200813167~173.5IrvineGGibsonIH.VFDrivesasFinalControlEle-mentsinthePetroleumIndustryJ.IndustryApplica-tionMagazine20028451~60.6FernandoJTEFongJACdeAlmeidaAT.Ecoanal-ysisofVariable-SpeedDrivesforFlowRegulationinPumpingSystemsJ.IEEETransactionsonIndustrialElectronics20115862117~2125.7CiontuMPopescuDMotocuM.AnalysisofEnergyEfficiencybyReplacingtheThrottleValvewithVaria-bleSpeedDriveCondensatePumpfromE.C.TurceniC.3rdInternationalSymposiumonElectricalandE-88440lectronicsEngineering.ISEEE2010293~2978.J.200725145~49.9.M.198933~35.10.J.20085971625~1630.11.M.3.200569~75.12.M.20055~13.13.J.2005257~59.14.J.2007291127~28.15.J.1999416334~338.16.Simulink/SimHydraulicsJ.201045631~34.ImpactofCentrifugalPumpVFConFlowControlPerformanceNIEJian-yingYUYangLUOXiong-linResearchInstituteofAutomationChinaUniversityofPetroleumBeijing102249ChinaAbstractIntheprocesscontrolboththrottlingregulationandvariable-frequencyregulationcanconstitutecentrifugalpump’sflowcontrolinfluidtransportsystem.Comparingitsvariable-frequencycontrolVFCwiththrottlingregulationshowsthatthethrottlingregulationasksformoreenergyconsumptiontogetherwithrelative-lysmallerdisturbedfluctuationandfasteradjustmentandthevariable-frequencycontrolencounterslowerdownstreampressurewhiletheflowgetslowerandthedynamicresponsetimeofvariable-frequencycontrolbe-comeslongerthanthatofthrottlingregulationwhiletheflow’ssetpointandthevesselpressurechangesudden-ly.DerivationandsimulationresultsshowthatVFChaslimitationinprocesscontrol.Keywordsflowregulationvariable-frequencycontrolthrottlingregulationcentrifugalpumpDCS。17177%89%DCS。。、、DCS20PID13315377%89%。17PID。。。。PIDPIDPID31。。DCS。9844.
本文标题:离心泵变频控制对流量控制性能的影响分析
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