您好,欢迎访问三七文档
当前位置:首页 > 行业资料 > 其它行业文档 > UBF厌氧反应器处理高pH值退浆废水的启动试验研究薄国柱
28 3Vol.28 No.320068JournalofHebeiInstituteofTechnologyAug.2006:1007-2829(2006)03-0134-04UBFpH1,2,3,3(1.,063009;2.,,210036;3.,210098):UBF厌氧反应器;退浆废水;快速启动;颗粒污泥 :重点研究采用UBF厌氧反应器难降解退浆废水的启动,试验结果表明,在中温(35±3℃)、进水COD为2000mg/L左右、HTR为24h、OLR为2.0kgCOD/m3d、pH7.6左右情况下2个月迅速启动,COD去除率稳定,并培养出适应水质要求厌氧颗粒污泥;经过YDT弹性填料和组合填料的挂膜比较发现:组合填料经YDT弹性填料挂膜快、三相分离效果好、COD处理效果组合填料经YDT填料高2%~8%。:X703 :A ,(、、、,)CODCOD60~70%,80%,,COD,50~55%,15%[1,2],PVA()、CMC(),PVA,,BOD5/CODcr0.064,(pH14),[3]。UBF(UASB)(AF),,UBF,,(OLR),UBF,,[4]。,。1 1.1 2UBF,90mm,1200mm,6.3L。,YDT,。,35℃,1。1.;2.;3.;4.;5.;6.;7.NaOH;8.;9.;10.PVC;11.1 UBF:2005-10-261.2 ,,。:COD4000~10000mg/L,BOD5400~2000mg/L,pH12~14,SO2-4120~270mg/L,NH3—N6.2-12.4mg/L,100-200。1.3 COD:;pH:pHpH;:;(VFA):;:;SS:;。1.4 ,UBF,2.5L。:(1-12d)、25%+(13-19d)、50%+(20-25d)、75%+(26-30d)100%(31-39d)。COD∶N∶P200∶5∶1,(HRT)24h,(OLR)2.0kgCODm3d。pH7.0,pH7.6。SRBMPB[5],pH,、、、pH(COD/SO42-42)。2 2.1 (COD)UBF(YDT)2,,,,CODcr80.2%;,,,,CODcr84.4%;、、,、,UBF,CODcr,:73.36%、71.87%、66.35%。UBF,。 2 (HRT=24h)CODcr/[SO42-4]=1.93,CODcr84.4%,,SO42-4UBF。、、、pH7.5,,UBF。2.2 YDTUBFCODYDTUBFCOD3。135 3 ,:UBFpH3,,COD,5d,UBFYDTUBF,14d,CODUBFYDTUBF8%,,,2%。 UBFYDTYDT,14d,,YDT。YDT,,,。2.3 UBF,,,1.0—2.0mm(4),,,PVA,TSS68.3g/L,VSS34.5g/L。2.4 UBF,,。(40d),,(15℃),12,,,HRT24,31%,,4d,COD65%。,。3 (1)COD2000mg/L、HTR24h、OLR2.0kgCODm3d、pH7.62、5,,,。、。(2)YDT:YDT、、。(3)UBF,。:[1] .—[M].:,2000.4.[2] HPWeberetal.—[J].,1997,(2):24-26.[3] ,.[M].:,2002.4.[4] Guio.tS.R.,andVandenBergL.,Performanceandbiomasretentionofupflowanaerobicreactorcombiningasludgeblanketandflitertrea-tingsugarwaste,BiotechnologyandBioengineering,1985,(27):800-806.[5] ,,,.[J].,2002,(18):18-22.136 28 Starting-upanAnaerobicUBFReactorforTreatingDesizingWastewaterBOGuo-zhu1,LUJi-lai2,CAOJia-shun3,CAIJuan3(1.CollegeofCivilEngineeringandArchitecture,HebeiPolytechnicUniversity,TangshanHebei063009,China;2.JiangsuInstituteofEnvironmentalScience,Nanjing,Jiangsu210036,China;3.SchoolofEnvironmentalScienceandEngineering,HehaiUniversity,NanjingJiangsu210098,China)Keywords: UBFreactor;desizingwastewater;quickstart-up;granularsludgeAbstract: Thearticleisfocusedonstart-upofanaerobicUBFreactorfortreatingpoordegradabledesizingwastewater.ThestartupofUBFreactor,thefiltermediumretainedthebiomassandthecultivationofanaerobicgran-ularsludgeadapttodesizingwastewaterwascompletedwithintwomonthperiod.ThestartupresultsofstudyshowedthatUBFreactorischaracterizedbyfaststartup,operationstableandeffectivetreatmentcapacityatatmiddletem-perature(35±3℃)、CODofinfluentisabout2000mg/L、HRTis24h、organicloadingrate(OLR)is2.0kg-CODm3dandpHisabout7.6.ComparedwiththeYDTfiltermediumandmixingfiltermediumfound,mixingfil-termediumwasveryeffectiveasagas-liquid-solidseparator,retainingbiomassbetterthanYDTfiltermediumandhigherCODremovalrateabout2%to8%thanYDTfiltermedium.(上接第133页)RemovalofNaturalOrganicMatter(NOM)inDrinkingWaterbyConventionalTreatmentProcessJIANGDeng-ling1,BOGuo-zhu1,NIGuo-wei1,XULi-li2,SUNShan-li2(1.CollegeofCivilandArchitecturalEngineering,HebeiPolytechnicUniversity,TangshanHebei063009,China;2.TangshanMunicipalWastewaterCo.Ltd,Tangshan,Hebei063000,China)Keywords: drinkingwater;naturalorganicmatter(NOM);nonpurgeableorganiccarbon(NPOC);assimilableorganiccarbon(AOC);removalefficiencyAbstract: Removalofnaturalorganicmatterindrinkingwaterbyconventionaltreatmentprocess(coagulation-sedimentation-sandfiltration)wasinvestigatedinnorthChina.AverageremovalefficiencyofCODMnbyconventionaltreatmentprocesswas16.7%.TheremovalefficiencywasinfluencedbytheconcentrationofCODMnofrawwaterandtemperature,whichwasbetterwhenthebothwerehigh.Removalefficiencyofnonpurgeableorganiccarbon(NPOC)was16.7%.Assimilableorganiccarbon(AOC)concentrationincreased55.3%aftertreatmentbecauseofchlorination.AverageAOCconcentrationoftreatedwaterwas160.63μg/L.Thedrinkingwatercannotmeetabiostabilitycriteriaof10μg/L.137 3 ,:UBFpH
本文标题:UBF厌氧反应器处理高pH值退浆废水的启动试验研究薄国柱
链接地址:https://www.777doc.com/doc-6542536 .html