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当前位置:首页 > 商业/管理/HR > 企业文化 > NaClO氧化去除高盐废水中氨氮的影响因素及其动力学研究方小琴
INDUSTRIALWATER&WASTEWATERVol.48No.2Apr.,20171,1,1,2(1.,200437;2.,200434):(201405267),。,(Cl-)1%,20~100mg/L,:NaClO,。:NaClO,NaClO、、、。NaClO0.6%,0.01575min-1。,,45mg/L,,。,2.0%,,,。,,10℃35℃,0.00188min-10.01043min-1。:NaClO;;;:X703.1:A:1009-2455(2017)02-0018-06InfluencingfactorsandkineticsofammonianitrogenremovalinhighsalinitywastewaterbyNaClOoxidationFANGXiao-qin1,HUJun-jie1,XIAJun-fang1,2(1.ShanghaiJingyuEnvironmentEngineeringCo.,Ltd.,Shanghai200437,China;2.ShanghaiNormalUniversity,Shanghai200434,China)Abstract:UsingNaClOoxidationtodegradeammonianitrogeninhighsalinitywastewater,theinfluencingfactorsandkineticsofthereactionwerestudied.Theresultsshowedthat,thedegradationprocessofammoniani-trogenbyNaClOfollowedpseudo-first-orderkineticsmodel,andtheinfluencingfactorsincludeddosageofNaClO,initialconcentrationofammonianitrogen,salinity,temperatureandsoon.WhentheNaClOdosagewas0.6%,thereactionratewasashighas0.01575min-1.Thehighertheinitialconcentrationofammonianitrogenwas,theworsetheeffectofoxidationreactionwouldbe.Whentheinitialmassconcentrationwasnotabove45mg/L;withtheincreasingofinitialconcentration,theinfluenceofitonoxidationrateconstantincreased.Lowsalinityhadlittleinfluenceonammonianitrogenoxidation,however,whenthesalinitywasover2.0%,theinhibitingeffectofitonammonianitrogenoxidationwouldbestrengthened,andthereactionrateconstantdecreaseddistinctly.In-creasingreactiontemperaturewasbeneficialtoammonianitrogenoxidationanddegradation.Duringtheprocessofthetemperatureincreasedfrom10℃to35℃,thereactionrateconstantincreasedfrom0.00188to0.01043min-1.Keywords:NaClOoxidation;highsalinitywastewater;kinetics;ammonianitrogenNaClO!!!!!!!!!!!!!!!!!!!!!!!!·18·100~300mg/L,[1-5]。NaClO,[6-7]。,,[8],,,NaClO。NaClO,,NaClO、、、,。11.1:NaClO(10%,CP)、NaCl()。:752、WTW3210pH、WTW330i。1.2,1。1.3NaClO,NaClOHClO,HClO(NH2Cl)、(NHCl2)(NCl3)。NCl3pH5.5,,2,NCl3[9]。[10-11]:NaClO+H2O→HClO+NaOH(1)NH3+HClO→NH2Cl+H2O(2)NH2Cl+HClO→NHCl2+H2O(3)NHCl2+H2O→NOH+2Cl-+2H+(4)NHCl2+NOH→N2↑+HClO+H++Cl-(5):2NH3+3NaClO→N2↑+3H2O+3NaCl(6),,NaClO1.5∶1,7.97∶1,,,1gNaClO7.97g。1.4200mL6,NaClO,,,,(NaClO);,,,;,,,;、,,,。1.5pH、,(Cl-),,CODCr。22.1NaClO43.6mg/L,CODCr250~300mg/L,1.0%,(25±1)℃,NaClO,1。1,NaClO,,,0.6%,180min,94.3%,,,。,NaClO0.6%,m(NaClO)∶m()=13.76∶1。1g7.97gNaClO,,NaClO。1,,,:lnC=lnC0-kt①1Tab.1ExperimentalwatercharacteristicspH/%ρ()/(mg·L-1)ρ(CODCr)/(mg·L-1)6.5~7.50.5~3.020~80250~300,,:NaClO·19·INDUSTRIALWATER&WASTEWATERVol.48No.2Apr.,2017ln(C/C0)=-kt②:C0———,mg/L;C———tmin,mg/L;t———,min;k———,min-1。ln(C/C0),t,2。2,NaClO,,。k3。3,NaClOk,R20.9790。NaClO0.3%0.6%,k0.00278min-10.01575min-1;NaClO0.8%,k0.01745min-1,。NaClO,,,NaClO,HClO,。2.2NaClO0.6%,CODCr250~300mg/L,1.0%,(25±1)℃,4。4,,。22.7~45.0mg/L,88.2%;45.0mg/L80.0mg/L,88.2%55.9%。,,45.0mg/L。5。5,,R20.98,k,6。 20406080100120140160180t/minρ()/(mg·L-1)504030201000.3%0.6%0.4%0.7%0.5%0.8%(a) 1NaClOFig.1EffectofNaClOdosageonammonianitrogenremoval20406080100120140160180t/min/%1008060402000.3%0.6%0.4%0.7%0.5%0.8%(b) 2NaClOFig.2ChangesofammonianitrogenconcentrationalongwithtimeunderdifferentdosageofNaClO20406080100120140160180t/minln(C/C0)0-1-2-3-4-50.3%,y=-0.00278x,R2=0.98990.6%,y=-0.01575x,R2=0.99800.4%,y=-0.00658x,R2=0.99280.7%,y=-0.01678x,R2=0.99900.5%,y=-0.01061x,R2=0.99550.8%,y=-0.01745x,R2=0.9972 3NaClOkFig.3EffectofNaClOdosageonreactionrateconstant(k)0.30.40.50.60.70.8NaClO/%k/min-10.0200.0150.0100.0050k=0.0185-(0.0051/CNaClO)·exp[-3.1668(lnCNaClO+1.0369)2]R2=0.9790·20· 6,R20.9450,。,,k,22.7mg/L80.0mg/L,k0.01872min-10.00430min-1。;45.0mg/L,,。2.343.6mg/L,NaClO0.6%,CODCr250~300mg/L,(25±1)℃,,7。7,0.5%~2.0%,,180min,19.6mg/L;2.0%~3.0%,,20406080100120140160180t/minρ()/(mg·L-1)100806040200(a)4Fig.4Effectofinitialconcentrationofammonianitrogenonitsremoval20406080100120140160180t/min/%10080604020022.7mg/L(b)45.0mg/L35.5mg/L80.0mg/L68.2mg/L55.0mg/L22.7mg/L45.0mg/L35.5mg/L80.0mg/L68.2mg/L55.0mg/L 5Fig.5Changesofammonianitrogenconcentrationalongwithtimeunderdifferentinitialconcentrationsofammonianitrogen20406080100120140160180t/minln(C/C0)0-1-2-3-4-522.7mg/L,y=-0.01872x,R2=0.995755.0mg/L,y=-0.00658x,R2=0.997935.5mg/L,y=-0.01564x,R2=0.996968.2mg/L,y=-0.00542x,R2=0.995645.0mg/L,y=-0.01161x,R2=0.989980.0mg/L,y=-0.00430x,R2=0.98026kFig.6Effectofammonianitrogenonreactionrateconstant(k)20304050607080C0/(mg·L-1)k/min-10.0200.0150.0100.0050k=exp[-(3.6189+0.0104C0+1.9526×10-4C02)]R2=0.9450 20406080100120140160180t/minρ()/(mg·L-1)45403530252015(a)7Fig.7Ammonianitrogenremovalunderdifferentsalinityconditions20406080100120140160180t/min/%60504030201000.5%2.5%1.0%2.0%1.5%3.0%(b)0.5%2.5%1.0%2.0%1.5%3.0%,,:NaClO·21·INDUSTRIALWATER&WASTEWATERVol.48No.2Apr.,2017,,180min,41.1%。,8。8,,R20.99,k,9。9,0.5%~2.0%,k;2.0%3.0%,,k0.00468min-10.00315min-1。2.0%,;2.0%,,,。Na
本文标题:NaClO氧化去除高盐废水中氨氮的影响因素及其动力学研究方小琴
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